Sierra 24v non starter...(after no start for 4 years)
Hi everyone,
Thought it was about time I done something with my project that has been left sitting for approx 4 years. I have a 1989 sierra xr4x4 with a 24v cosworth installed.
The background. The engine was installed, and ran and drove, before being parked up for further work to be done on the car.
the problem now? It won't start. I checked the oil levels(and topped up) and other basics before attempting a start after 4 years standing, new battery, fresh fuel. After a extra boost from a second battery the starter turned it over, but no start. So. I have spark, I have fuel as the plugs are wet after cranking, the crankshaft sensor tested and confirmed as working, checked I have 12v on the edis6 at pin8, and I appear to have 12v ignition on pins 37 and 57 on the ecu. I removed the air filter and duct. Last time today when I was fiddling around, I gave it one last try and I had a loud pop and bang and a reasonably substantial amount of smoke through the air intake/filter...
Sooo.... my question. Has something internal just made a bigger problem or am I missing something?is it timing?i didnt think the chain could jump.i wanted to confirm the engine was good before starting the rest of the resto on the car. To add, while it's sat nothing has been done to the car, it has just sat, as is.
am grateful for any ideas/guidance.
thanks
Mark
Thought it was about time I done something with my project that has been left sitting for approx 4 years. I have a 1989 sierra xr4x4 with a 24v cosworth installed.
The background. The engine was installed, and ran and drove, before being parked up for further work to be done on the car.
the problem now? It won't start. I checked the oil levels(and topped up) and other basics before attempting a start after 4 years standing, new battery, fresh fuel. After a extra boost from a second battery the starter turned it over, but no start. So. I have spark, I have fuel as the plugs are wet after cranking, the crankshaft sensor tested and confirmed as working, checked I have 12v on the edis6 at pin8, and I appear to have 12v ignition on pins 37 and 57 on the ecu. I removed the air filter and duct. Last time today when I was fiddling around, I gave it one last try and I had a loud pop and bang and a reasonably substantial amount of smoke through the air intake/filter...
Sooo.... my question. Has something internal just made a bigger problem or am I missing something?is it timing?i didnt think the chain could jump.i wanted to confirm the engine was good before starting the rest of the resto on the car. To add, while it's sat nothing has been done to the car, it has just sat, as is.
am grateful for any ideas/guidance.
thanks
Mark
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